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Sorry to hear it man. I know how it feels for I blew my motor too last yr in my vortech AT g35. I was pushing over 400hp tho and had redline mine when it blew. How much timing did they add to your tune bc there must have been a reason why u're tune was only up to 5500 and not to redline. U're best bet is to do a tear down and see how the pistons looks (detonations, etc) to determine if it was a weak rod or a tunning issue. Hopefully your heads are okay so u don't have to buy a longblock. GL
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wow dude.. sorry to see that. hopefully you'll be back up and running soon.
btw: was the tune conservative? i'm wondering about your timing also. what was your fuel setup like? oil level full too? |
sorry to hear this happen bro. but at least you had 14k miles of good fun
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sorry to hear that, just makes me wonder what the inside of my engine looks like at this point. good luck on whatever steps you take.
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WTF!! NO!!!!!!!!!!!!!! Damn that sucks to hear bro, update us on exactly what happened. Also, you think any of this has to do with the Procharger, no right?
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yeah i know, but if its because of the procharger then im 1 step closer to having to go tt =) I always had 2nd thoughts on the procharger thats why....
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alot of motors have blown running the ATI, do a search on my350z. I think Greddy TT and ATI may be top contenders...
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damn dude that sucks with so little miles..... I have a short block off an 03 if you need...
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Sounds like your rod went through the oil pan. I have had this happen with a 97 GS-R. I was running a Turbonetics Kit and the same thing happened....driving home from hanging out with some friends....loud clank followed by a pop and an oil trail about a 1000 feet long....and clouds of smoke. Sorry to hear man. This just makes me change my mind more and more about boosting the G.
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