My Twins R going 2 Performance Factory
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My Twins R going 2 Performance Factory*UPDATE*
well folks....as some of you may know i've been having trouble with my car.my motor spun a bearing on the dyno last year and i had my motor built by Nigel at premeire performance...problem was that he used 11 to 1 comp. ratio forged pistons and i kept blowing my head gasket on the dyno after that.I recently bought an 05 auto motor w/18k miles on it. I had a friend of mine who works for Warren Henry Infiniti pull it apart and build it with cp 8:5 to 1 comp ratio forged pistons,eagle rods arp head stud, cometic head gaskets etc. so far i've put 1200 miles on the motor and have been talking to Jeremy about installing the u-tec and tuning the car for me! Well......my day is THURSDAY!!!My goal is to hit the 500 rwhp # but Will settle for anything close to that.....I believe Jeremy is the man to help me achieve these #'s as i've watched and read countless threads about the great work he does!
wish me luck everyone and i'll be sure to update everyone with the results!
Winston.
P.S. I chose not to go into all the details with my problems at Premiere and Nigel because it would take way too long to explain!
wish me luck everyone and i'll be sure to update everyone with the results!
Winston.
P.S. I chose not to go into all the details with my problems at Premiere and Nigel because it would take way too long to explain!
Last edited by Silver-Bullit; 03-23-2007 at 10:45 AM.
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#12
hey guys, winston is HAULing a$$ back to miami, we spent well over 12 hours today on the dyno and basically sorted through minor problem after minor problem that was with his car. mostly fuel related...
the car really needs to be given some TLC with someone (me) who cares about doing stuff correctly. winston is a very cool guy and deserves his car running top notch.
after getting all the fuel issues worked out, we werent able to make any power over 9 psi due to either A: coupling leaking, B: exhaust manifold leaking pre turbo or 3: a vaccuum line issue.
we simply didnt have enough time to work our way through the all the small stuff.
car runs great on 9 psi though and put down around 400 all day. the car could make 14 psi but no power increase due to one of the small issues.
i drove it though and it felt very strong for 9 psi and i am sure winston will be happy till he has a chance to spend another day here.
THANKS for all the nice comments guys and watch out for a blue Z here soon!!!
the car really needs to be given some TLC with someone (me) who cares about doing stuff correctly. winston is a very cool guy and deserves his car running top notch.
after getting all the fuel issues worked out, we werent able to make any power over 9 psi due to either A: coupling leaking, B: exhaust manifold leaking pre turbo or 3: a vaccuum line issue.
we simply didnt have enough time to work our way through the all the small stuff.
car runs great on 9 psi though and put down around 400 all day. the car could make 14 psi but no power increase due to one of the small issues.
i drove it though and it felt very strong for 9 psi and i am sure winston will be happy till he has a chance to spend another day here.
THANKS for all the nice comments guys and watch out for a blue Z here soon!!!
#13
Originally Posted by audiblemayhem
hey guys, winston is HAULing a$$ back to miami, we spent well over 12 hours today on the dyno and basically sorted through minor problem after minor problem that was with his car. mostly fuel related...
the car really needs to be given some TLC with someone (me) who cares about doing stuff correctly. winston is a very cool guy and deserves his car running top notch.
after getting all the fuel issues worked out, we werent able to make any power over 9 psi due to either A: coupling leaking, B: exhaust manifold leaking pre turbo or 3: a vaccuum line issue.
we simply didnt have enough time to work our way through the all the small stuff.
car runs great on 9 psi though and put down around 400 all day. the car could make 14 psi but no power increase due to one of the small issues.
i drove it though and it felt very strong for 9 psi and i am sure winston will be happy till he has a chance to spend another day here.
THANKS for all the nice comments guys and watch out for a blue Z here soon!!!
the car really needs to be given some TLC with someone (me) who cares about doing stuff correctly. winston is a very cool guy and deserves his car running top notch.
after getting all the fuel issues worked out, we werent able to make any power over 9 psi due to either A: coupling leaking, B: exhaust manifold leaking pre turbo or 3: a vaccuum line issue.
we simply didnt have enough time to work our way through the all the small stuff.
car runs great on 9 psi though and put down around 400 all day. the car could make 14 psi but no power increase due to one of the small issues.
i drove it though and it felt very strong for 9 psi and i am sure winston will be happy till he has a chance to spend another day here.
THANKS for all the nice comments guys and watch out for a blue Z here soon!!!
-sean
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WOW....is basically all i can say!!! my drive back home from Perfomance Factory to miami was FUN!!Let me start off by saying that if anyone of you guys that HAVE NOT put the U-TEC in your car and have it tuned by Jeremy......U are missing out on alot of power! I've been twin turboed for one year now with the e-manage blue and have blown the original motor TWICE like i stated above but NEVER has my car felt like this with LESS hp than what i Dynoed on the e-mange! It's a totally different car!
I also need to let it be known that my day @ the Factory was great 1st class treatment from Jeremy and his crew (big ups to Matt and his Sweet lookin Z! and Eric for the mulitple trips the the parts store!)Victor with his Wicked Azz honda!
next for me is to put t-bolts all around run new vacuum lines and check for leaks and TURN UP THE BOOST!
later.
Winston.
I also need to let it be known that my day @ the Factory was great 1st class treatment from Jeremy and his crew (big ups to Matt and his Sweet lookin Z! and Eric for the mulitple trips the the parts store!)Victor with his Wicked Azz honda!
next for me is to put t-bolts all around run new vacuum lines and check for leaks and TURN UP THE BOOST!
later.
Winston.
Last edited by Silver-Bullit; 04-05-2007 at 10:30 PM.